and during renovation repainted in gray. Used to be the Homestead High-Level Bridge. Other famous thing that happened here was the crash of a B-25 in the 50's into the Mon River near the bridge. The plane was never found. Speculation was it was carrying something secret - a nuke? And was lifted in secret out of the river by the government.
Since DU'ers love :tinfoilhat: How does a whole aircraft disappear and never be found in a river that is not that wide nor that deep?
In the middle of the afternoon on January 31, 1956 a B-25 bomber crash-landed into the Monongahela river near Homestead, Pennsylvania. All six aboard survived the impact, though two of them died before they were saved from the cold water. It was an unfortunate accident, and in the following weeks a search for the sunken plane was conducted.
The odds of finding the plane seemed pretty good - at the crash location the river was only 500 to 1,000 feet in width and 25 to 35 feet in depth. In comparison, a B-25 bomber is 52 feet long, 17 feet tall and has a wingspan of 67 feet. It took 15 minutes to sink underwater, and there were plenty of witnesses, so its last location above water was well known. It did not seem that finding the bomber would be a difficult task; yet after two weeks of hard searching, the plane was still missing and the operation was abandoned. So where did the B-25 really go?
The conspiracy theories flew fast and loose on this mystery. The most popular story was that the plane secretly carried some important, confidential cargo and was recovered incognito by the government. Anything from nuclear bombs to aliens were said to be inside the plane. As such, in the middle of the night a squad of elite government cover-up men retrieved the plane from the river, and had it shipped away. There were, of course, eyewitnesses who saw this secret operation. And the public search? Nothing but a hoax to cover for the real rescue. Oh, there was also an undercover seventh member of the crew who was pulled from the river. And Glenn Miller was aboard, they flew into the Bermuda Triangle, and…
Courtesy Pittsburgh Post-GazetteLike most conspiracy theories, it's rather preposterous. The government's side of the story is both less ridiculous and less intriguing. According to military representatives, the plane was carrying no secret cargo - instead, it was to deliver two people to Harrisburg, as well as pick up airplane parts. Due to a malfunction the plane ran out of fuel on the way to its destination. The crew tried to turn around and get to a nearby airport, but by the time they realized they were under-fueled they were just too far away. The engines sputtered to a halt over the Mon, and the pilot crashed it there.
http://www.damninteresting.com/?p=579#more-579Major Dotson advised the crew that the aircraft would be ditched in the river. Captain Jamieson transmitted a "Mayday" which was overheard at the Allegheny County Tower at 1609E on either 126.18Mc or 257.8Mc. Major Dotson lowered wing flaps and completed a wheels-up touchdown, heading downstream in a generally south, southwest direction at approximately 1610E to 1611E. The ditching was successful and all occupants evacuated the aircraft with no apparent injuries. all six persons were able to climb aboard the upper surfaces of the aircraft as it floated down the stream. The Monongahela river at this point varies from 500 to 1000 feet in width; the river depth varies from 25 to 35 feet. The current was estimated to be approximately 8 to 10 knots; the recorded water temperature was 35 degrees F; the recorded air temperature was 27 degrees F; the recorded wind velocity was 8 to 10 knots, from the northwest. The aircraft remained afloat for an estimated 10 to 15 minutes.
...that the aircraft was sinking, the crew and passengers to remove their shoes and swim to a log observed floating nearby. ...all six persons could swim. Sergeant Alleman, Airman Smith and Major Dotson reached the nearby log successfully, Major Dotson and Airman Smith remained with the log until recovered by a commercial river boat, approximately 15 minutes later. Master Sergeant Alleman reached the log but struck out for the left bank of the river. He was able to swim ashore with great difficulty and was assisted from the water by civilians and local police officers. Captain jamieson was able to remain afloat until recovered by a police launch.
Captain Ingrahm disappeared beneath the water. Sergeant Soocey was on some unidentified debris when last seen. The aircraft drifted for an estimated 1 mile from the point of impact prior to sinking. Major Dotson and Airman Smith, the last personnel to be recovered were recovered approximately 1 1/2 to 2 miles from the scene of impact. At the time of this report neither the aircraft nor missing personnel have been located.
http://www.caterpillarclub.org/b25/b25.htm